2nd Generation Specific 1986-1992 Discussion

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Old Jun 22, 2011 | 04:29 AM
  #11  
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If you think about it. Having 2 injectors that don't fire is a long shot that it's a problem with both injectors. The common link is the ECU as it is what completes the ground for the injectors. So it was a grounding issue through the ECU and once I swapped them out it ran perfect. I have a USDM ....ECU in there now instead of the JDM and it works just fine.
Old Jun 22, 2011 | 05:14 AM
  #12  
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this is what fixed my car. I had a spare ECU laying around for an S5 turbo
Old Jun 22, 2011 | 08:22 PM
  #13  
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good deal yea its hard to make a call if its actually the ecu or not and if you got a spare one thats the best thing right there
Old Jun 22, 2011 | 10:05 PM
  #14  
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i ran a compression test... i got no compression in the back rotor... gonna pull the motor friday
Old Jun 23, 2011 | 12:05 AM
  #15  
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are you getting anything out of it cause it could be a stuck seal
Old Jun 23, 2011 | 01:01 AM
  #16  
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i go nothing on the rear rotor. if i remove the gauge i can hear a wooshing (with the motor turning over) but nothing on the gauge, tryed it twice to verify
Old Jun 23, 2011 | 01:08 AM
  #17  
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did you have a strange sound before it stopped working
Old Jun 23, 2011 | 01:16 AM
  #18  
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i bought the car with it not working. it sat for 9 years. it only has 64,000 miles (1987 turbo II)
Old Jun 23, 2011 | 02:01 PM
  #19  
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well sitting for 9 years isnt good most likely the coolant seals went and flooded the rear
Old Jun 23, 2011 | 02:32 PM
  #20  
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Originally Posted by RicerJ
well sitting for 9 years isnt good most likely the coolant seals went and flooded the rear


Yeah. I'll know more thus weekend when I pull it apart



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