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THE QUEST FOR 500

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Old 03-11-2012, 05:01 PM
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Default Re: THE QUEST FOR 500

more side housing shots. the resize is making the photos look like garbage wtf? how do you get a full size pic on?
Attached Thumbnails THE QUEST FOR 500-side-housing-2.jpg   THE QUEST FOR 500-side-housing-3.jpg  
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Old 03-12-2012, 10:13 AM
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Default Re: THE QUEST FOR 500

now that is open. do some balancing and rotor clearance
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Old 03-14-2012, 11:28 PM
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there were no signs of the rotors hitting the plates.
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Old 06-14-2012, 07:58 PM
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UPDATE on the re-build , I got it reassembled and am breaking it in with currently 300 miles on it . I still had a small random miss at idle ( it has had since i bought 7 years ago) which i thought was normal, i changed out to ls coils just because i was still suspicious of the ignition. sure enough the miss is gone and its the smoothest i have ever felt it, it gained vac and i can run afrs in the 13.5 to 14.0 range at idle before i could only ger 12.5 out of it before it would start to die. its also taking more fuel through out the rpm range. I will post more updates after a full breakin and full boost runs have been made !
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Old 07-25-2012, 10:23 PM
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car has been running great untill the last couple days , its been 95 or so latley and if i drive it for atleast an hour it will start to sputter under heavy load. the afrs go lean and 02 feedback starts to compensate but it almost feels like ignition again. the only thing thats changed since the rebuild is the coil setup, its now a sequential system with ls-1 coils at 6ms dwell. it took 6ms to get 45kv out off them and without it the car would reak up under boost . sorta stumped on it its hard to believe thats its the coils but i just dont know what else would be so heat dependent ? any thoughts would be appreciated
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Old 07-27-2012, 12:04 AM
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on a side note car still breaks up at 25 psi... foud ot that my alt is almost putting out 1.0 volt ac at 5k . not sure ifthis is my breakup but its def a problem. more money into the bottomless pit .
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Old 07-28-2012, 02:43 PM
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did some data logging and the battery volts were dropping to 12.6 at redline and would idle at 13.7 . i decided to put a new alt on it and while i was in there seperate the alt +lead away from the cas wires . i also re-routed my coil trigger wires as far away from the alt and cas as possible . I hate to get ahead of my self but it appers to have fixed it entirely . upon start up i noiticed it was running leaner. the batt voltage stayed at 14.5 at idle and would drop to 13.7 at red line . ac voltage stayed at .225 to .30 all the way up to redline. i got the boost up to 29 psi without break up and made 6-7 pulls with no issues . I'm crossing my fingers and hope it stays the way it is for more than a week !!!!!!!!!!!
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Old 07-30-2012, 09:51 PM
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the car is now running worse than ever after 20 min of driving. starts to misfire and act like the timing is off. the boost gauge starts rising to 4-5 psi and bucking violently just while trying to make it off the road . it was so bad that my whole exhaust including the dp was glowing orange. seriosly thinking about just parting this pos out
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Old 07-30-2012, 11:59 PM
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id leave it to the guys in the workshop before you go any further. 10 points for trying but at the end of the day if u blow another engine you wont be having any fun for a while.
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Old 07-31-2012, 09:13 AM
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thats he sad thing i am the work shop. this is what i do for a living and im at a loss of words. there have been very few cars that i havent been able to fix in the years and the fact that its my own erks me
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