Fb W/ T2 Motor Dynoed At 212whp
after tunning the car on the street took it to the car to the dyno to do any of the fine tune adjustments and to see what power we would put down. the boost controller was having trouble controlling the boost spool up of the stock turbine. the exhaust had little restriction and the boost just wanted to go as high as it wanted to go, the profec didnt have its job cut out for it
. the intake charge pipe was of a small diameter and i think was quite a restriction even for a stock setup. the intercooler was mounted in frotn of the raidator but was only slightly bigger then stock. this was on 10 psi
owner: June
relevant mods:
stock port s4 jspec engine
haltech e6k
2.5" DP, 3" after
custom IC
t2 coils
9's on all 4 plugs
owner: June
relevant mods:
stock port s4 jspec engine
haltech e6k
2.5" DP, 3" after
custom IC
t2 coils
9's on all 4 plugs
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