3rd Generation Specific Talk about 3rd gen RX-7's here.

woo fixed my fd's stumble/lack of fuel

Old May 16, 2007 | 05:50 PM
  #1  
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yea so anyway, not that i said anything, but my fd was having major issues in low vaccuum situations (aka about 12psi of vac to 0) basically in all rpms it would stutter and stumble. so i hooked up the lm-1 and saw major lean-out. So i added more fuel across the low vac areas, no change if anything it got worse, added more fuel nothing. finally got to the point where it was almost undrivable. So at work I decided that since the fuel pressure was good it must be a fuel volume issue, thats why the more fuel i asked for the worse it would get.



So my walbro has been whiney since I installed it, I've had walbros before and it seemed a lot more whiney then I had remembered. So I figured well if im going to replace the fuel filter anyway (generally the cause of a fuel volume problem when the pump is new) I might as well pull out the walbro, double check everything and check the fuel filter sock.



I pulled the walbro and holy **** that sock was disgusting, filled with crap. Cleaned it out real good put it back on and swapped out the fuel filter at the same time. The fuel filter seemed relatively new and showed no signs of blockage. But now the walbro doesnt whine at all and I have 0 stutter/lean-out problems.



The car runs like a freaking indy car now, and I'm still not even close to boosting it.



So lesson learned, when a car sits for 3-4 years, even if you drop in a new pump with a new filter on it, the crap in the tank can still build up into enough of a problem that it leaves you wondering.



Back to your regular programming.



kevin.
Old May 16, 2007 | 06:57 PM
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i had the same problem with my 240... but i actually had to change the whole tank because it was so gunked up
Old May 16, 2007 | 07:16 PM
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glad somebodys fd is getting some use...
Old May 16, 2007 | 09:52 PM
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yeah my fd has gone thru a few filters and a pump since its been out of the bodyshop...
Old May 17, 2007 | 12:15 AM
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man thats one of those situations where your like damn I never knew It would be such a big but easy to fix problem. Glad to hear things are working better for you now.
Old May 17, 2007 | 01:39 AM
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Shame on you for not cleaning your gas tank on a single turbo FD...
Old May 17, 2007 | 08:31 AM
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cleaning the gas tank? meh doesnt really matter until i go anywhere near boost anywho, as I said, im no where near boost, and with the leanout situation i was barely nearing 10psi of vaccuum.



but yea anyway today or tomorrow im dropping the tank and flushing it anywho, no biggie, i only drive it maybe 10 miles a day, if that.



also the fact that the fuel filter showed zero signs of having any grime in it shows that the particles in the tank are simply too large to make it past the fuel pump sock, anything that makes it past the pump would show up in the filter, nothing showing up in the filter means nothing making it past the pump.



but yea anywho, guess i should finish my t2 now.



kevin.
Old May 17, 2007 | 10:03 AM
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Just bustin' your ***** Kevin. lol
Old May 17, 2007 | 06:26 PM
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yea I know , sorry if it came out wrong, i was just detailing my plans lol.



stupid filter sock is starting to clog up again, i can hear it start whining.



vaccuum tuning is going nicely though



kevin.
Old May 17, 2007 | 10:11 PM
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You just reminded me to replace my fuel filter.

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