2nd Generation Specific 1986-1992 Discussion

A holidy tragedy

Thread Tools
 
Search this Thread
 
Old 12-27-2005, 09:36 AM
  #1  
Senior Member
Thread Starter
 
One320B's Avatar
 
Join Date: May 2005
Posts: 959
Default

Well I went back home for the xmas weekend and met up with a buddy of mine yesterday who also came home from TX. He had ordered a full racing beat exhaust for his N/A a few weeks ago as well as a new driveshaft and was planning to put it on over the weekend. When he got home, one of his xmas gifts is that his old man actually installed everything already. Pretty sweet deal if you ask me. His dad doesn't know much about the rx7s, but did a great job during the install. One exhaust hanger was a little worn out so the drive muffler hung a little low, but other than that it looked great. I swung out by their hangar(where the car was being worked on) to see the car and catch up with him. Well while I was there he flushed out the tranny fluid, put some nice redline fluids in, had new spark plugs, and did a quick oil change. He was gearing the car up to be driving back from VA to TX. Started it up...had really bad idle, wouldn't hold the idle at all when cold...backed it from the hangar and started to let it warm up...still ran rough and wouldn't idle. We went to drive it to get it warmed up and check everything out. The racing beat exhaust sounded really quiet, but had an awesome tone to it. Anyways, while driving the car had NO power, I mean NONE..it decelled on the uphills...i started making jokes that his compression was low from the car sitting for last few years (it was driving a few months ago, but for the most part it just sits). Drove around, went back to the house....started checking the obvious..no vac leaks, TB secondaries were working properly... the aux ports though were stuck, but the car never went above 4K during our drive, so it wasn't like we needed those to really work anyways.. to sum this long story up...we pulled the spark plugs from the front rotor...cranked it...three really good puffs of air..best i've heard in a while! ...pulled the rear plugs... nada, zip, no compression... 1986 Base N/A Rx7 w/ 183K original miles finally gave up the ghost. he's going to try MMO thinking that maybe the seals are just stuck from sitting...but we're both pretty sure it's done. The car is in great shape, paint is only a few years old, interior is spotless for it's age... and he already has another motor, but now he has to tow it to TX..



I've got pics/vids/etc that I'll try and get up. It's just nice to see a rotary w/ 183K still crank up and run, even if it is one rotor...
One320B is offline  
Old 12-27-2005, 02:10 PM
  #2  
Senior Member
 
teknics's Avatar
 
Join Date: Dec 2002
Location: Wayne, NJ
Posts: 4,837
Default

keep at it, if its been siting for a while that happens, hell it happens when it hasnt been siting for too long sometimes as well.



my n/a ran great, sat for two days, and then the rear rotor lost compression. luckily i decided to try to go get gas for it and all of a sudden it backfired on the way there and bam it ran perfectly.



it was weird, but i dont mind it since it came back to working condition fine .



kevin.
teknics is offline  
Old 12-27-2005, 02:36 PM
  #3  
Senior Member
Thread Starter
 
One320B's Avatar
 
Join Date: May 2005
Posts: 959
Default

Yea, I mean..we are pretty good with these engines by now..and we know there is a chance it'll come around w/ some MMO thats why he's giving it a shot..but w/ 183K miles on the ticker...it'll just be borrowed time anyways... He just wants to be able to drive it back to TX instead of paying a tow bill...
One320B is offline  
Old 12-27-2005, 02:37 PM
  #4  
Senior Member
Thread Starter
 
One320B's Avatar
 
Join Date: May 2005
Posts: 959
Default

Oh, but the funnier thing is his luck has been bad all month. He has a '91 T2 also that he just built the motor for after going through two junk atkins motors...ran it on the dyno, put down crap numbers..so now he has to dig around the haltech and find that missing power.. just not going good for him this month...
One320B is offline  
Old 12-27-2005, 10:40 PM
  #5  
Senior Member
 
sweet7's Avatar
 
Join Date: Jun 2003
Location: Stacked outside you're trailer door
Posts: 1,430
Default

Sorry to hear about it. But the life you got outta that motor, you cant complain too much!
sweet7 is offline  
Old 12-28-2005, 12:35 AM
  #6  
Senior Member
 
drftk1d's Avatar
 
Join Date: Apr 2004
Location: NY
Posts: 403
Default

yeah, 180k out of any car is alot
drftk1d is offline  
Old 12-28-2005, 04:37 AM
  #7  
Member
 
NHDrifterFC's Avatar
 
Join Date: Mar 2005
Location: Nashua, NH
Posts: 42
Default

210,000 on my odometer... but maybe thats why my car wont start anymore....
NHDrifterFC is offline  
Old 12-28-2005, 07:08 AM
  #8  
Super Moderator

 
banzaitoyota's Avatar
 
Join Date: Jul 2002
Location: My BIG ol TURBO-DIESEL
Posts: 5,181
Default

Pull a DR. HO on it!
banzaitoyota is offline  
Old 12-28-2005, 11:48 AM
  #9  
Senior Member
 
j9fd3s's Avatar
 
Join Date: May 2002
Location: California
Posts: 22,465
Default

my gsl-se did that, the corner seal springs were literally pounded into the rotors. everyone thinks just cause the tach stops at 8k that its got some kinda rev limiter....
j9fd3s is offline  
Old 12-28-2005, 12:30 PM
  #10  
Senior Member
Thread Starter
 
One320B's Avatar
 
Join Date: May 2005
Posts: 959
Default

Lol... the best I ever saw was an '88AE w/ 220K miles on it.. it didn't run at the time, but still...it must have had at least 200K on it when it still ran..no way they put 20K miles on a blown motor.





I'm gonna check on the car later this week to see if he got it running or not..
One320B is offline  



All times are GMT -5. The time now is 12:47 AM.